Earlier this year I sent my 87GT out to Gabe Anderson for a 7730 conversion. I’ve had everything for the swap, but just never got around to it when someone was available. Gabe did the conversion and from what I understand, it fired up on the first try.
I’ve been driving it for a few months and really enjoying it. Took it on the RFTH 27 Scouting Run and got to play with some Porches on The Rattler but during that run, it developed a loud whine in the drivetrain. Since the trans already had a faint whine, I guessed that was the issue. Having previously bought another Getrag, I opted to just go ahead and have it swapped in. New Luk clutch kit at the same time.
When Scott dropped the drivetrain out, he found that the right drive axel had a ripped CV boot and all the lube was gone. THAT was probably where the noise came from. The axel was only about 14 months old. So, in the process, a new axel was installed, too.
Once everything was out, we found that the engine had been running so lean that the exhaust manifold had turned black from the heat and had cracked beyond compare. The muffler that had a loose baffle had also blown a gaping hole in it. So, a replacement exhaust system was secured from The Fiero Farm in St. Stephens, SC. Just prior to turning the car over to Scott, I had upgraded the injectors because I found that the engine was running too lean. However, I couldn’t see the damage it had caused. There were other indications of a lean burn and when I researched the injectors, I found that the rebuilder had listed them as 17# when they were actually 14# injectors.
Another consequence of the lean fuel mixture is that it welded the o2 sensor into the fitting on the crossover pipe. Days and days of heating and soaking with penetrating oils were of little help. Eventually, it came out, but it left half the threads from the sensor in the fitting. Scott luckily had the exact tap (the largest he had) to clean out the threads for a new sensor.
As the 7730 harness work was disconnected and pulled back through the firewall, we apparently pulled some wires loose. That was a big issue for a bunch of us who knew nothing about repining, even though we had Sinister Performance’s pinouts.
It took a lot of work to get things sorted out with Sinister Performance being very patient and helpful to answer the many questions I put to him. Scott, Steve, Michael, Jay, and Roger all had a hand in sorting things out. Even with the whole village fixing a Fiero, we missed some things. A few days ago, we found a pair of wires that hadn’t been grounded. It got rid of some trouble codes but may have caused some other codes to come about. That’s yet to be determined.
As the exhaust system was reinstalled, the crossover pipe changed positions and with everything back in place, we couldn’t get the coil pack and ICM to mount in their original location. Scott devised a method to elevate it about 3 inches to clear the Digital EGR Solenoid and its mounting base. It’s still in the same place, but just sitting a little higher.
Some of the wiring looms had melted due to the extremely high heat in the engine bay that was caused by the lean burn. The plastic wire loom melted to the wires and some wires were even damaged. We got some High-Temperature Nylon wire loom from Pat, and Scott replaced the wires that were damaged or questionable. Some things were rerouted just in case the newer wire loom wasn’t sufficient to protect the wiring circuits.
This is a list of most of the things done to the car.
Clutch replaced
Transmission replaced
Cracked firewall side exhaust manifold discovered and replaced
Blown out muffler discovered and replaced
Torn CV boot discovered and axle replaced
Coil spring rubber isolators replaced
Electronic EGR valve wiring replaced and rerouted
Crank sensor wiring replaced and rerouted
Various wire looms replaced
A fusible link at the C500 had begun to melt. Replaced
Spacers placed under coil pack
Connectors were placed in various ECM to allow for wiring harness removal
7730 conversion wiring mistakes corrected
Code 42 eliminated
AC high-pressure Schrader replaced
AC wiring corrected
AC low-pressure switch replaced
AC refrigerant leak corrected
AC recharged and functioning correctly
o2 sensor replaced
Might be another detail or two that were missed.
Pictures of the project will be edited into the thread a few at a time.